燃料与化工 ›› 2020, Vol. 51 ›› Issue (2): 43-46.

• 煤气净化与化学产品加工 • 上一篇    下一篇

煤焦油加氢装置升级为劣质柴油加氢改质装置的方案研究

黄云1  张凯2   

  1. 1.胜帮科技股份有限公司, 上海201210;2.易高生物化工科技(张家港)有限公司, 苏州215600
  • 出版日期:2020-03-23 发布日期:2020-03-24

Study on the feasibility of upgrading from coal tar hydrogenation plant to inferior diesel hydrogenation plant

Huang Yun1  Zhang Kai2   

  1. 1.Spang Technology Co.,Ltd.,Shanghai 201210,China; 2.ECO Biochemical Technology (Zhangjiagang) Company Limited,Suzhou 215600,China
  • Online:2020-03-23 Published:2020-03-24

摘要: 介绍了16 万t/a煤焦油加氢装置升级改造为劣质柴油加氢改质装置的方案,分析了改造可能存在的技术及设备瓶颈,经改造增加循环氢脱硫系统、加氢进料泵、脱硫化氢汽提塔及柴油分馏塔底泵后,可年加工44 万t劣质柴油。经技术经济评价分析,改造后总加工成本为532 元/t柴油。

关键词: 煤焦油, 升级改造, 劣质柴油, 加氢

Abstract:

In this paper,introduction is made to the proposal of upgrading from 160,000 t/a coal tar hydrogenation plant to inferior diesel hydrogenation plant.Bottlenecks possibly occurring in technique and in equipment during the modification are analyzed.The modification will have additional desulfurization system by circulating hydrogen,hydrogenation feed pump,H2S stripper and pump at bottom of diesel fractionating column,this upgraded plant will have capacity of refining 440,000 t inferior diesel per year.It’s reported in technical and economic evaluation that after the modification,the operating cost is totaled at ¥532 Yuan for refining per ton of diesel.

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